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Elkem
Metals Alloy: Major Smelter Sets Production Records After Implementing
New Computer System
By
Phillip G. Richardson, IT Manager, Elkem Metals

Elkem's Alloy, West Virginia plant produces nearly
30 percent of all the silicon metal consumed in
North America.
Tucked
into the West Virginia hills and along the New River about 45 minutes
southeast of Charleston is the small, unincorporated town of Alloy.
It is home to the largest silicon metal smelter in North America. The
smelter operates around the clock, every day of the year. It produces
360,000 to 380,000 pounds of high-grade silicon metal a day, which represents
nearly 30 percent of all industrial and commercial demand in the United
States, Canada and Mexico.
Since
a new computer system was installed in the mix house, production records
have been set on each of our five furnaces. We could not have set these
new records without a solid flow of material through the furnaces, and
the new MODCOMP system that assured us of that uninterrupted flow.
In
the autumn of 1996, we transferred our mix house process system from
a proprietary operating system, MAX IV, to REAL/IX operating system,
MODCOMP's real-time implementation of the UNIX System V operating system
for 88K-based REAL/STAR platforms.

Object-oriented touch screen is key to successful
real-time process control in the mix house of Elkem Metals'Alloy,
West Virginia facility. Steve Bainer, mix house dispatcher, monitors
process.
We
had two primary reasons for the switch: we did not have the personnel
to modify the software on the old system by adding features or equipment;
and the new system improves our mix house control and eliminates delays
without any outages in the system. This is important to us because we
have no redundant computer system.
The
raw material in our smelting process is dirt-nearly 2 million pounds
a day. We start out with rock, coal and woodchips and we make high-grade,
high-purity silicon metal that goes to chemical, consumer product and
electrical and electronic manufacturers. We must maintain a stable flow
and consistent blending of materials into the furnaces to achieve stable
performance and efficiency. Today, the combination of the REAL/IX operating
system and application software written by AccessWare controls the mix
house, where the smelting process begins with the blending of material.
This blending is one of the most significant aspects to our process.
Our
process is controlled by a fusion of old and new technologies. Some
tasks are accomplished through manual processes. For example, an operator
in a huge front-loader tractor literally pushes raw materials into the
furnaces. At the other end of the technology scale, operators monitor
fully-automated processes on touch screens that provide information
displays.
The
success of this conversion was marked by the stable REAL/IX operating
system and the object-oriented data system application software. These
tools allow us to use object-oriented design philosophy to maximum benefit.
Previously,
if we had a system outage with full demand on all five furnaces, we'd
have to manually run mix to each of them for about one full shift to
give the automated system time to catch up before we could go back to
full mix control. With the new system, it takes the system only two
hours to catch up after a full outage.
We
evaluated writing proprietary software and testing it on a parallel
computer system at one of our plants. We calculated it would cost $200,000
and take at least six months to develop and test the software.
We
wanted faster turnaround, so we submitted the project for bids. Proposals
ranged from $200,000 to $800,000. Most of them involved PCs running
some sort of object-oriented display control system (SCADA) with programmable
logic controllers (PLCs). The greatest problem with all those proposals
was that it would require us to shut down the plant for several weeks
to install the new system.
Then
MODCOMP came up with a proposal to use a REAL/IX-based computer with
an interface that would allow us to transfer to the new system for testing,
and transfer back to the previous system if required. It took only two
minutes to shut down one system and activate the other system.
Operations
have been smooth since the day we brought the new system on-line in
October 1996. We have to give credit to an exceptional design provided
by AccessWare, our project integrator. With the application software
running on the UNIX-based platform, we have positive command control
over every element of the process. There's no guesswork involved.
Real-time
control is especially important to us. When you're controlling a 30
MW furnace, any malfunction requires immediate action. We can't afford
a system that takes time to determine a solution.
We
need a system that acts on a priority interrupt immediately, and can
support hundreds of interrupt items.
Further,
real-time monitoring is important to control raw materials, and that
includes the electricity that powers the furnaces. If we interact and
control that efficiently, we save money. On the other hand, we cannot
always predict with total accuracy the nature of our raw material stream.
There's a lot of potential for variation, so the computer system needs
to allow for that as well.
The
biggest challenges we have in implementing any new process technology
is that we don't have much time for off-line training because we have
a continuous process. We needed an object-oriented design interface
that was intuitive, so an operator who knows our process intimately
could adapt this tool and make effective use of it with a minimum of
training.
At
this point, we know we have achieved a successful integration. If we
didn't, we could not have set our recent production records.
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